When I hooked up my shift linkage I had the pan off so I got the mechanism dead in the middle where it is supposed to be. I have a picture too!!! (Not that it helps) But I had to jumper it anyway as it didn't ground through the NS switch. I also set up the kickdown by looking at it internally when the pan was off to see at what points the button inside is depressed and I marked it on the trans case. (Again, not that it helps) Then I put the throttle at WOT and pulled the Lokar cable so that it completely pulled the kickdown all the way back and clamped it that way.
So when I hit WOT the arm is all the way back! This however leaves it about halfway back under idle. On the test drive I found it felt like the trans was dragging and it did not want to shift out of 1st. It did a couple times and then it hit very hard.
I suspect the kickdown should not be depressed at idle? But if will only be about halfway depressed at WOT if it isn't. I can't believe I should need more travel in the linkage as it isn't any different than stock travel. As for the shift adjust, I think I just need to
take a continuity tester under the car and re-adjust using it.