Rich, Sounds like you've been down the road on projects like this before. Two comments, first; do not rely on WD40 as a lubricant, it has solvents features that help in cleaning but it primarily a moisture displacer, great if you have moisture in your distributer cap. If you want to lube something use Breakfree or one of the other quality oils. Second, you asked for a grease reccomendation, Lubriplate is an excellent choice or some of the new synthetic greases as speced by some of the automobile companys will do a great job. Jim faber South Carolina > > From: Rich Barber <barber@xxxxxxxxx> > Date: 2005/05/31 Tue PM 01:07:59 EDT > To: Chrysler 300 Club International Yahoo Server <Chrysler300@xxxxxxxxxxxxxxx> > Subject: [Chrysler300] 1955 C-300 Power Seat Repair and Gearbox Lube > > I spent the afternoon getting the power seat in my 1955 C-300 to work. > Before, it would just click, but not move. I'm sharing my findings and > procedure below, but have a question first. > > Page 201 of the 1955 Chrysler service manual states: "The vertical > power unit shaft is equipped with a ball nut and should not be > lubricated. The horizontal power unit shaft is equipped with a friction > nut that is packed with life-time grease requiring no further > lubrication." Additionally there is a gearbox on the horizontal power > unit where a small worm gear drives and rotates the worm drive power > unit shaft. If that gearbox was also packed with "life-time grease", > its life-time is over and the grease is gone, having leaked out and and > accumulated on the exterior of the gearbox and assembly and attracted 50 > year's worth of dirt and dust bunnies.. Anyone have a recommendation > for what kind of grease to pack that little gearbox with? > > Findings and Procedure: > > Inoperation was partially due to a buildup of crud on various rotating > elements, especially the 3/4" (?) worm gears that position the links and > torque rods. With the assemblies removed and the motors direct fed from > the battery, nothing would rotate until disassembled, cleaned and lubed. > > Inoperation was also partially due to one of the two switches not > feeding a ground in one position as it should. > > The ground cable was disconnected from the battery. > > The front seat bottom can be removed by just lifting it up. Pretty > handy! Looks like a plumber's and electrician's nightmare under there, > but you don't have to understand the complex mechanical linkage to work > on the system. > > The six wires connected to the switch were tagged and removed. This > enabled checking the various switch positions for continuity. One > position was dead on the vertical switch, so the seat could not be moved > down after being sent all the way up. Jumpering a ground to the relay > enabled reversing the motor. It was possible to clean the worm drive > power shaft of the vertical unit without removing the power unit by > spraying with WD-40 and ragging it off. So only repair of the switch > was required > > Both switch positions worked ok for the vertical power unit and produced > relay clicking at the motor but no rotation. > > The steel and aluminum surround at the driver's side of the seat base > was removed by removing four small sheet metal screws holding it to the > seat frame. This enabled access to the three screws holding the switch > assembly to the surround.. > > The surround was cleaned and the aluminum polished. The steel part of > the surround needed repainting with black enamel, that for another day. > > The switches are serviceable, sort of. Each of the two switches is held > in the chrome pot metal housing by two spring steel clips. I ended up > breaking the clips to get the bad switch out of the housing. Once out > and cleaned, it became apparent the black plastic switch body was held > together with small wire clips that were sort of like big square > U-shaped staples. These clips were easy enough to remove and enabled > the inside mechanism and contacts to be accessed. One of the sets of > contact points had enough erosion and corrosion to prevent electrical > contact. Not having any contact cleaner, I just polished all the points > with a little brass detailing brush and reassembled the switch using the > two wire clips. Much like filing a set of ignition points. > > Not having replacements for the broken spring steel clips, I just jammed > a couple of steel brads into the spaces where the clips would have > gone. This seemed to do a good job of securing the switch in the > housing. Time will tell how long this crude fix lasts. > > I removed the vertical power unit after first removing two small snap > rings from the mounting pins. This task required a snap-ring tool with > tiny points. The relay box was removed after tagging the wires. The > relay functions checked out ok. The wires from the switch provide > grounds to the relay and cause high-amp hot current to flow to the > armature and one or another of the fields of the motor. There are three > wires coming from each motor. The two smaller wires are fields, one for > each direction. The larger wire is the armature connection. To test > the motor, I bolted one field wire to the armature wire and connected > these two wires to the Negative (Hot) side of my 6-Volt battery. Then > connecting the Positive (ground) side of the battery to the body of the > motor. After completely removing the motor from the gearbox, The motor > started and ran fine in both directions. (Whew!--what a relief--don't > have to go shopping for a motor.). After cleaning the worm drive power > rod and the gearbox, they were reassembled to the motor and the system > worked fine in both directions with direct power from the battery. > There was a large rubber flex coupling between the end of the motor > shaft and the small worm gear driving the power rod. I think some of > the accumulated crud was surrounding the coupling and preventing rotation . > > Reassembly went fine. The seat can be levered as needed to allow the > power unit to be slipped over the two mounting pins. I WD-40'd the > connection points on the linkage and torque levers. > > Reconnected the battery ground cable and everything worked fine. The > motors ran smoothly and quietly. Cleaned and buffed the leather seat > base while it was out. Also vacuumed the carpet under the seat. > > Now that the power seat works, I can install the seat belts I bought > last year. I have sure felt naked without them and > she-who-must-be-obeyed will not ride in the car without them. One old > report on the 1955 Chrysler 300 said the car cornered better than the > driver, what with the slick leather seats. Not so bad when you have a > steering wheel to hang on to, but there is no panic bar for the > passenger to grab. > I hope this may be helpful to anyone with inoperative power seats. The > bottom line is they are a complex electro-mechanical system, but can be > services with simple tools and unskilled labor. I assume they are > pretty much the same in later years. Consultations available and > criticisms welcomed. > > C-300'ly, > Rich Barber > Brentwood 94513 > > > > > > To send a message to this group, send an email to: > Chrysler300@xxxxxxxxxxxxxxx > > For list server instructions, go to http://www.chrysler300club.com/yahoolist/inst.htm > Yahoo! Groups Links > > > > > > > ------------------------ Yahoo! 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